Main Title |
Field tests of industrial stoker coal-fired boilers for emissions control and efficiency improvement, site F / |
Author |
Langsjoen, Peter L. ;
Tidona, R. J. ;
Gabrielson, J. E.
|
Other Authors |
|
CORP Author |
KVB, Inc., Minneapolis, MN.;Industrial Environmental Research Lab., Research Triangle Park, NC.;Department of Energy, Washington, DC. Div. of Power Systems.;American Boiler Manufacturers Association, Arlington, VA. |
Publisher |
The Office ; Available to the public through the National Technical Information Service, |
Year Published |
1980 |
Report Number |
EPA-600/7-80-065a; DOE-EF-77-C-01-2609 |
Stock Number |
PB80-183023 |
OCLC Number |
07097930 |
Subjects |
Coal--Combustion--Environmental aspects ;
Furnaces--Combustion--Environmental aspects
|
Additional Subjects |
Air pollution control ;
Boilers ;
Stokers ;
Particle size distribution ;
Industrial wastes ;
Combustion products ;
Oxygen ;
Carbon dioxide ;
Carbon monoxide ;
Nitrogen oxide(NO) ;
Nitrogen dioxide ;
Sulfur dioxide ;
Hydrocarbons ;
Sampling ;
Equipment ;
Design ;
Field tests ;
Concentration(Composition) ;
Fly ash ;
Sulfur trioxide ;
Air pollution sampling
|
Internet Access |
|
Holdings |
Library |
Call Number |
Additional Info |
Location |
Last Modified |
Checkout Status |
EJBD |
EPA 600-7-80-065a |
c.1 |
Headquarters Library/Washington,DC |
09/17/2013 |
EKBD |
EPA-600/7-80-065a |
|
Research Triangle Park Library/RTP, NC |
01/16/2004 |
ELBD ARCHIVE |
EPA 600-7-80-065a |
Received from HQ |
AWBERC Library/Cincinnati,OH |
10/04/2023 |
NTIS |
PB80-183023 |
Some EPA libraries have a fiche copy filed under the call number shown. |
|
07/26/2022 |
|
Collation |
vi, 107 pages : illustrations ; 28 cm. |
Abstract |
The report gives results of field measurements made on an 80,000 lb/hr coal-fired spreader-stoker boiler. The effects of various parameters on boiler emissions and efficiency were studied. Parameters included overfire air, flyash injection, excess air, boiler load, and coal properties. Measurements included O2, CO2, CO, NO, NO2, SO2, SO3, HC, controlled and uncontrolled particulate loading, particle size distribution of the uncontrolled flyash, and combustible content of the ash. In addition to test results and observations, the report describes the facility tested, coals fired, test equipment, and procedures. Particulate loading on this unit averaged 6.00 lb/million Btu uncontrolled and 1.05 lb/million Btu controlled at full load. Nitric oxide emissions averaged 0.45 lb/million Btu (330 ppm) at all loads. |
Notes |
"Industrial Environmental Research Laboratory, Office of Environmental Engineering and Technology, Research Triangle Park, N.C." Mar. 1980. "IAG/contract nos. IAG-D7-E681 (EPA), EF-77-C-01-2609 (DoE), program element no. EHE624." |
Place Published |
Washington, D.C. Springfield, Va. |
Supplementary Notes |
Sponsored in part by American Boiler Manufacturers Association, Arlington, VA. See also report dated Dec 78, PB-293 731. |
Access Notes |
Also available via the World Wide Web. |
Corporate Au Added Ent |
United States. Department of Energy. Division of Power Systems. Energy Technology Branch.; United States. Environmental Protection Agency. Office of Energy, Minerals, and Industry.; Industrial Environmental Research Laboratory (Research Triangle Park, N.C.); American Boiler Manufacturers' Association. |
Title Ser Add Ent |
Research reporting series. Interagency energy-environment research and development ; EPA-600/7-80-065 a. |
PUB Date Free Form |
1980 |
Series Title Untraced |
Interagency energy/environment R & D program report ; EPA-600/7-80-065a |
NTIS Prices |
PC A06/MF A01 |
BIB Level |
m |
Medium |
unmediated |
Content |
text |
Carrier |
volume |
Cataloging Source |
OCLC/T |
OCLC Time Stamp |
20130618074149 |
Language |
eng |
SUDOCS Number |
EP 1.23/8:600/7-80-065 a |
Origin |
OCLC |
Type |
MERGE |
OCLC Rec Leader |
02240cam 2200409Ia 45020 |