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RECORD NUMBER: 4465 OF 4742

Main Title Three-Stage Combustion (Reburning) Test Results from a 300-MWe Boiler in the Ukraine.
Author LaFlesh, R. C. ; Lewis, R. D. ; Hall, R. E. ; Kotler, V. R. ; Mospan, Y. M. ;
CORP Author ABB/Combusion Engineering, Inc., Windsor, CT. ;All-Russian Heat Engineering Inst., Moscow. ;Ladyzhin Power Station (Ukraine).;Environmental Protection Agency, Research Triangle Park, NC. Air and Energy Engineering Research Lab.
Publisher 1993
Year Published 1993
Report Number EPA-68-02-4280; EPA/600/J-93/235;
Stock Number PB93-236644
Additional Subjects Afterburning ; Air pollution abatement ; Boilers ; Staged combustion ; United States ; Russia ; Ukraine ; Nitrogen oxides ; Performance evaluation ; Design criteria ; Coal-fired power plants ; Reprints ; Foreign technology
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NTIS  PB93-236644 Some EPA libraries have a fiche copy filed under the call number shown. 07/26/2022
Collation 21p
Abstract The paper gives results of a program to design, install, and test a natural-gas three-stage combustion (reburn) system on a 300-MWe, opposed-wall, wet-bottom (slagging) coal-fired utility boiler operating in the Ukraine. The U.S. EPA sponsored this program in support of a working group initially involving the EPA and (the former) Soviet Union, and now consisting of representatives from the EPA, Russia, and the Ukraine. The host boiler fires a high volatile Ukrainian bituminous coal, a Siberian brown (lignite) coal, or various blends. An opposed-wall, natural-gas reburn system was designed and installed in the summer of 1992. Parametric testing was carried out during the remainder of 1992. Initial parametric test results from this boiler show average nitrogen oxide (NOx) reductions of about 50% from a baseline pre-retrofit level of 600 ppm, corrected to 3% oxygen (0.82 lb NOx/million Btu). During this testing, variations in boiler operation and conditions resulted in a range of NOx reductions of 40-60%. Additional testing and analysis is currently in progress to define the results further and to optimize system performance.
Supplementary Notes Presented at Environmental Protection Agency/Electric Power Research Institute Symposium on Stationary NOx Control, Miami, FL., May 23-27, 1993 and AFRC Meeting, Tulsa, OK., October 18-20, 1993. Prepared in cooperation with All-Russian Heat Engineering Inst., Moscow, and Ladyzhin Power Station (Ukraine). Sponsored by Environmental Protection Agency, Research Triangle Park, NC. Air and Energy Engi
NTIS Title Notes Rept. for Nov 88-Apr 93.
Title Annotations Reprint: Three-Stage Combustion (Reburning) Test Results from a 300-MWe Boiler in the Ukraine.
Category Codes 68A; 81A; 97R; 97J; 97I
NTIS Prices PC A03/MF A01
Primary Description 600/13
Document Type NT
Cataloging Source NTIS/MT
Control Number 330926039
Origin NTIS
Type CAT