Main Title |
EPA evaluation of Bahco industrial boiler scrubber system at Rickenbacker AFB / |
Author |
Biedell, E. L. ;
Ferb, R. J. ;
Malamud, G. W. ;
Ruff, C. D. ;
Stevens, N. J. ;
|
Other Authors |
|
CORP Author |
Industrial Environmental Research Laboratory (Research Triangle Park, N.C.) |
Publisher |
Environmental Protection Agency, Office of Research and Development, Industrial Environmental Research Laboratory. |
Year Published |
1978 |
Report Number |
EPA-600/7-78-115; F33617-75-90100 |
Stock Number |
22161 |
OCLC Number |
04942886 |
ISBN |
pbk. |
Subjects |
Scrubber (Chemical technical) ;
Boilers
|
Additional Subjects |
Scrubbers ;
Air pollution control equipment ;
Electric power plants ;
Sulfur dioxide ;
Flue gases ;
Boilers ;
Particles ;
Cost analysis ;
Performance evaluation ;
Sludge disposal ;
Solid waste disposal ;
Operating costs ;
Performance tests ;
Particulates ;
Stationary sources ;
Limestone scrubbing ;
Coal fired power plants ;
Venturi scrubbers ;
Rickenbacker Air Force Base
|
Internet Access |
|
Holdings |
Library |
Call Number |
Additional Info |
Location |
Last Modified |
Checkout Status |
EKBD |
EPA-600/7-78-115 |
|
Research Triangle Park Library/RTP, NC |
12/05/2003 |
ELBD ARCHIVE |
EPA 600-7-78-115 |
Received from HQ |
AWBERC Library/Cincinnati,OH |
10/04/2023 |
ESAD |
EPA 600-7-78-115 |
|
Region 10 Library/Seattle,WA |
03/23/2010 |
NTIS |
PB-286 611 |
Some EPA libraries have a fiche copy filed under the call number shown. |
|
07/26/2022 |
|
Collation |
223 p. : ill. ; 28 cm. |
Abstract |
A comprehensive test program which characterized the particulate removal, sulfur dioxide removal, operating costs, maintenance costs, waste product properties operating experience and capacity of a size 50 R-C/Bahco scrubbing system installed to treat flue gas from coal fired boilers at Rickenbacker AFB, Columbus, Ohio, was completed. Tests were conducted over an 18 month period during which 27,216 tons of coal were burned. The results from this program demonstrate that this system is capable of controlling both particulate and sulfur dioxide emissions from the combustion of high sulfur (2-4%) mid-Western coal at firing rates from 20 MM to 200 MM Btu/hr. A cost of $4.27 per ton for optimum operation with limestone was projected. Waste product properties relative to dewatering handling and disposal were found to be similar to those measured for other FGD waste products. |
Notes |
Prepared for Environmental Protection Agency, Office of Research and Development. Interagency energy agreement no. D5-0718, program element no. EHE624A. June 1978. |