Record Display for the EPA National Library Catalog

RECORD NUMBER: 29 OF 1341

OLS Field Name OLS Field Data
Main Title Advanced waste treatment for housing and community developments /
Author Bodwell, Russell.
CORP Author Levitt and Sons, Inc. Greenwich, CT.;Municipal Environmental Research Lab., Cincinnati, OH. Wastewater Research Div.
Publisher Municipal Environmental Research Laboratory, Office of Research and Development, U.S. Environmental Protection Agency,
Year Published 1978
Report Number EPA-600/2-78-168; EPA-68-01-0077
Stock Number PB-287 827
OCLC Number 04440120
Subjects Sewage disposal--United States. ; Sewage sludge. ; Sewage disposal. ; Sewage sludge. ; United States.
Additional Subjects Sewage treatment ; Coagulation ; Sedimentation ; Filtration ; Adsorption ; Chlorination ; Performance evaluation ; Solid waste disposal ; Sludge disposal ; Cost analysis ; Design criteria ; Residential buildings ; Physical chemical treatment ; Sludge treatment
Internet Access
Description Access URL
http://nepis.epa.gov/Exe/ZyPDF.cgi?Dockey=9101EMMQ.PDF
Holdings
Library Call Number Additional Info Location Last
Modified
Checkout
Status
EJAD  EPA 600/2-78-168 Region 3 Library/Philadelphia, PA 06/02/2000
EJBD ARCHIVE EPA 600-2-78-168 Headquarters Library/Washington,DC 07/22/2014
EJBD  EPA 600-2-78-168 Headquarters Library/Washington,DC 07/29/2013
EKAM  EPA-600/2-78-168 Region 4 Library/Atlanta,GA 01/17/1997
ELBD RPS EPA 600-2-78-168 repository copy AWBERC Library/Cincinnati,OH 10/17/2014
ESAD  EPA 600-2-78-168 Region 10 Library/Seattle,WA 11/07/1997
NTIS  PB-287 827 Most EPA libraries have a fiche copy filed under the call number shown. Check with individual libraries about paper copy. NTIS 06/23/1988
Collation xii, 141 p. : ill.
Abstract
Treatment of wastewater from a subdivision in a physical-chemical treatment plant (screening, chemical coagulation, sedimentation, filtration, carbon adsorption, chlorination) was evaluated. The 190 cu m/day (50,000 gal/day) plant was housed in the shell of a standard house on a standard lot in a 127 home subdivision. During the 18 month evaluation period excellent treatment was achieved (99% removal of BOD5, Suspended Solids, and Total Phosphorus). Shock loadings had almost no effect on plant performance because an equilization tank leveled out peaks and because of the ability of the physical-chemical processes to absorb excess loading. Extensive data on temporal characteristics of wastewater from a subdivision were collected during the evaluation. An experimental sludge filter and fluidized bed incinerator were installed to process the sludge but were not extensively used. The former did not function, the latter suffered from repeated mechanical breakdowns. Sludge was periodically hauled to a landfill by a septic-tank-hauler. Acceptance of the presence of a sewage treatment plant in the midst of the subdivision was excellent. No complaints of any type were registered by the homeowners. The system cost was higher than for a conventional plant. The actual construction cost exceeded $300,000 and operational expenses were greater than $0.53 per cubic meter ($2.00 per 1000 gallons). At the measured flow of 206 gal per home per day this represents a cost of $0.40 per home per day. It is anticipated that significant reductions in these costs would result from a redesign based on the experiences gained during the demonstration period.
Notes
Contract no. 68-01-0077.