Record Display for the EPA National Library Catalog

RECORD NUMBER: 34 OF 212

OLS Field Name OLS Field Data
Main Title Demonstration of Wellman-Lord/Allied Chemical FGD technology : acceptance test results /
Author Adams, R. C. ; Lutz, S. J. ; Mulligan, S.W.
Other Authors
Author Title of a Work
Lutz, S. J.
Mulligan, S. W.
CORP Author TRW, Inc., Durham, NC.;Industrial Environmental Research Lab., Research Triangle Park, NC.
Publisher Environmental Protection Agency, Office of Research and Development, Industrial Environmental Research Laboratory ; For sale by the National Technical Information Service,
Year Published 1979
Report Number EPA-600/7-79-014a; EPA-68-02-1877
Stock Number PB-290 514
OCLC Number 05017456
ISBN pbk.
Subjects Flue gases--Desulfurization. ; Flue gases--Desulphurization
Additional Subjects Air pollution control ; Sulfur dioxide ; Boilers ; Coal ; Flue gases ; Combustion products ; Industrial wastes ; Energy consumption ; Performance evaluation ; Tables(Data) ; Wellman process ; Flue gas desulfurization
Internet Access
Description Access URL
http://nepis.epa.gov/Exe/ZyPDF.cgi?Dockey=9101E3EK.PDF
Holdings
Library Call Number Additional Info Location Last
Modified
Checkout
Status
EJBD ARCHIVE EPA 600-7-79-014a Headquarters Library/Washington,DC 07/03/2013
EKAM  EPA-600/7-79-014 Region 4 Library/Atlanta,GA 08/19/1994
EKBD  EPA-600/7-79-014a Research Triangle Park Library/RTP, NC 12/12/2003
ESAD  EPA 600-7-79-014A Region 10 Library/Seattle,WA 03/23/2010
NTIS  PB-290 514 Most EPA libraries have a fiche copy filed under the call number shown. Check with individual libraries about paper copy. NTIS 06/23/1988
Collation ca. 150 p. in various pagings : ill. ; 28 cm.
Abstract
The report gives results of acceptance tests of Wellman-Lord/Allied Chemical flue gas desulfurization (FGD) technology. Process performance guarantees were met or exceeded. During the 12-day Design Load test, the plant was operated at the design condition of a boiler flue gas output rate equivalent to 80% of the maximum boiler load of 115 MW gross. During the 83-hour High Load test, the plant treated flue gas volumes equivalent to 95% of maximum boiler load. SO2 removal of 90% or better was achieved. Particulate emissions did not exceed 0.1 lb/million Btu of boiler heat input. The consumption of steam, natural gas, and electrical power was less than the performance guarantee requirements at Design Load conditions. Soda ash consumption was less than the limit set by the performance guarantees. Finally, sulfur product purity was greater than 99.5%.
Notes
Contract no. 68-02-1877, program element no. EHE624A. Prepared for U.S. Environmental Protection Agency, Office of Research and Development. Jan. 1979. Includes bibliographical references.