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RECORD NUMBER: 14 OF 532

Main Title Adipic Acid Enhanced Flue Gas Desulfurization Process for Industrial Boilers: Volume 1. Field Test Results Project Summary.
Author Clarke, P. A. ; Gerstle, R. W. ; Henzel, D. S. ; Mason, K. W. ; Sabatini, S. R. ;
CORP Author Industrial Environmental Research Lab., Research Triangle Park, NC.;Department of Energy, Washington, DC.
Year Published 1983
Report Number EPA-600/S7-82-065a-V.1; AI01-80EV10473;
Stock Number DE85016812
Additional Subjects Adipic Acid ; Flue Gas ; Sulfur Dioxide ; Air Pollution Control ; Boilers ; Coal ; Field Tests ; Lime-Limestone Wet Scrubbing Processes ; Removal ; ERDA/010800 ; ERDA/500200 ; ERDA/200202
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https://nepis.epa.gov/Exe/ZyNET.exe/2000TU8X.TXT?ZyActionD=ZyDocument&Client=EPA&Index=1976+Thru+1980&Docs=&Query=&Time=&EndTime=&SearchMethod=1&TocRestrict=n&Toc=&TocEntry=&QField=pubnumber%5E%22600S782065A%22&QFieldYear=&QFieldMonth=&QFieldDay=&UseQField=pubnumber&IntQFieldOp=1&ExtQFieldOp=1&XmlQuery=&File=D%3A%5Czyfiles%5CIndex%20Data%5C76thru80%5CTXT%5C00000004%5C2000TU8X.TXT&User=ANONYMOUS&Password=anonymous&SortMethod=h%7C-&MaximumDocuments=10&FuzzyDegree=0&ImageQuality=r75g8/r75g8/x150y150g16/i425&Display=p%7Cf&DefSeekPage=x&SearchBack=ZyActionL&Back=ZyActionS&BackDesc=Results%20page&MaximumPages=1&ZyEntry=1&SeekPage=x
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NTIS  DE85016812 Some EPA libraries have a fiche copy filed under the call number shown. 07/26/2022
Collation 8 p.
Abstract
Test results show that adding adipic acid to the limestone slurry significantly improved the SO sub 2 removal efficiency of the FGD system. Limited baseline data on operations with limestone only indicated a performance level of 55% SO sub 2 removal. Adding about 2200 ppM of adipic acid to the limestone scrubbing systems, the unit's level of performance increased to an average of 94.3% SO sub 2 removal which was maintained within a standard deviation of 2.2% over a 30-day test period during which boiler load was 70 to 130 million Btu/hr and gas throughput varied 300%. (ERA citation 10:043665)