Main Title |
Performance evaluation of an industrial spray dryer for SO2 control / |
Author |
Kezerle, James A. ;
Mulligan, Steve W. ;
Dayton, Dave-Paul ;
Perry, Patricia J.
|
Other Authors |
|
CORP Author |
TRW Environmental Engineering Div., Research Triangle Park, NC.;Industrial Environmental Research Lab., Research Triangle Park, NC. |
Publisher |
U.S. Environmental Protection Agency, Industrial Environmental Research Laboratory : Cincinnati, OH : Center for Environmental Research Information [distributor], |
Year Published |
1981 |
Report Number |
EPA/600-S7-81-143; EPA-600/7-81-143; PB82-110701; EPA-68-02-3174 |
Stock Number |
PB82-110701 |
OCLC Number |
09468064 |
Subjects |
Flue gases--Desulfurization ;
Sulfur dioxide ;
Spray drying
|
Additional Subjects |
Air pollution control ;
Sulfur dioxide ;
Spray drying ;
Performance evaluation ;
Flue gases ;
Industrial wastes ;
Combustion products ;
Boilers ;
Particles ;
Fabric filters
|
Internet Access |
|
Holdings |
Library |
Call Number |
Additional Info |
Location |
Last Modified |
Checkout Status |
EKBD |
EPA-600/7-81-143 |
|
Research Triangle Park Library/RTP, NC |
02/27/2004 |
ELBD ARCHIVE |
EPA 600-S7-81-143 |
In Binder Received from HQ |
AWBERC Library/Cincinnati,OH |
10/04/2023 |
NTIS |
PB82-110701 |
Some EPA libraries have a fiche copy filed under the call number shown. |
|
07/26/2022 |
|
Collation |
9 pages : illustrations ; 28 cm. |
Abstract |
The report gives results of a test to evaluate the SO2 removal performance of the lime-spray-dryer/fabric-filter system treating flue gas from the stoker-coal-fired boiler at Celanese's Amcelle plant in Cumberland, MD, in August/September 1980. Continuous monitors were used to collect data according to EPA procedures for compliance testing. Data were collected for 23 days with the boiler operating at about half load. In addition to evaluating SO2 removal by dry flue gas desulfurization, operating experience with the boiler and spray-dryer/baghouse system was obtained for 5 months, ending September 30, 1980. Data were reduced to express SO2 removal on a mass per unit energy input basis as prescribed by EPA. Test results showed the mean SO2 removal efficiency to be 70% (standard deviation of + or - 9%) when the sulfur content of the bituminous coal averaged 2%. This efficiency generally was 60-80%, except during system upsets. During the last week of testing, daily SO2 removal averaged about 80%. System availability was 73% over the 25 days of testing and 96% over the last week. Report appendices provide data and computer averages for SO2 removal and the computer program used for data reduction. |
Notes |
Caption title. At head of title: Project summary. "Dec. 1981." "EPA/600-S7-81-143." Includes bibliographical references. |